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Restoration diary

Reports of restoration work on 50029 and 50030.

Announcement of working party dates and details of restoration work carried out at working parties.

June 20th 2010

Due to various reasons, we decided to cancel the last work party. This weekend Ian and Pete made a list of parts needed to complete the top end engine overhaul so they can hopefully be ordered this week from the supplier. They then continued refitting the new big end shells we had in stock, temporarily using old nuts on the stretch bolts, as we wait for more new ones. Finally, with the help of Dave and forklift truck, they brought the remaining overhauled heads round from the shed, ready for refitting to the power unit. Tim, Dom, Chris B, Chris T & Dave moved a significant amount of the items in the shed into our newly-acquired second BG for storage. Mark B brought two car loads of spares he has been keeping in his garage to also go into the new coach. I finished laying in the control wiring for the reverser, and started tidying up the loose wiring with lots of cable ties

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May 22nd 2010

We cancelled the last work party as it was the diesel gala and we had been told there would be no yard access. Today, Ian & Pete torqued down two more cylinder heads, but as they were working on the side of the power unit next to Renown, they found access difficult for the four-foot long torque multiplier, so just tightening two heads down to 600 ft lbs of torque took virtually all day. I sweltered inside Repulse finishing connecting the cables onto the main neutral terminal bar, then started sorting the control cables for the reverser. I also compared a large 1000mfd electrolytic capacitor (the size of a large baked beans tin) that I have been loaned, with ones we have on the input boards for the KV10's, to see if they will fit, and I found they did. We need four of these capacitors per KV10 input board, but as ours have not been used in at least 10 years, I have been advised they will probably no longer function, and I have been trying to source replacements. We had an unexpected call for help from Peak Rail in the afternoon, as one of the P.Way gang fell of a rail wagon and sustained possible hip, neck or back injuries, and we assisted the ambulance crew carrying the man to the ambulance.

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April 25th 2010

Dave continued cleaning & painting the second turbo, and yesterday examined the two remaining turbos on the power unit & found they both rotate freely, which is good news. Ian & Pete torqued down two cylinder heads to 600fpt, then examined the camshafts in the power units still in the locos to see if they were in better condition than the section that has some water damage in the ex-008 unit, but found both sections examined were in similar condition due to having stood idle for so long, so an off-site repair is looking likely. Chris Bodell continued his dirty work cleaning the clean air compt at No1 end, and has almost finished the one side now. I continued wrestling with the field divert cables, but found one marked for the one position that appears about two feet too short, so this will need further investigation.

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April 11th 2010

Ian, Pete, Chris T & Tom washed down both locos for their appearance at the upcoming PR diesel gala & by the end of the day, both locos looked pretty good. Chris B has taken on the unenviable task of cleaning debris from the No.1 end clean air room, and by close of play it was difficult to see where his overalls stopped and his head started! Dave Rolfe has dismantled and freed off the stuck turbo and is now cleaning and painting it. I fitted the last two missing sections of 185mm cable to the field divert resistors, and spent the rest of the day wrestling with the six 3mtr lengths that drop down to the reverser, as they need to be fitted in a certain order to avoid having them tangled, which requires fitting and removal multiple times until you get it right, not that easy due to the confined space of the thin-man's passage and they are quite stiff due to their size.

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March 28th 2010

On arrival at Peak Rail today, we discovered copper thieves had cut the four cables under No.2 end bogie to one of the traction motors. Two Peak Rail coaches had also been vandalised. This was reported to PR management. After examining Repulse, we discovered no other obvious damage & the other five motors seem to have escaped untouched. Ian, Pete & Dave stripped the seized turbocharger & removed both sets of bearings & although the shaft would move slightly along its axis, it stubbornly refuses to rotate, so this will be investigated further next workparty. I continued sorting & fitting the cables to the field divert contactors & resistors, discovering we are two lengths short, but have several duplicate surplus lengths which have been marked with their positions & could be used as spares or for Renown.

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